1. Background
A Regulatory (WHO-GMP/USFDA) compliant pharmaceutical manufacturing unit operates 28 AHUs under a centralized chilled water system. Environmental control (temperature, RH, pressure cascade) is critical for:
- tablet compression
- coating
- granulation
- packing rooms
- raw material sampling
Operators routinely adjust AHU valve positions based on comfort complaints from production staff.
2. Problem Observed
Multiple rooms showed:
- fluctuating room temperature (±3°C)
- high relative humidity during peak hours
- failure to maintain pressure differentials
- inconsistent product room conditions during validation checks
BMS trends showed:
- chilled water valve staying at 100% for long durations
- unexpected bypass flow
- low coil delta-T (only 2–3°C instead of 6–7°C)
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💚 Join Our WhatsApp Channel3. Operator Misconception Identified
Root misconception
“Keeping bypass partially open ensures continuous chilled water flow, avoids coil choking, and improves cooling.”
Operators believed:
- bypass must never be fully closed
- closing the bypass increases risk of airlock
- keeping valve in manual mode gives faster cooling
- pressure fluctuations are harmful to AHU coils
To “solve” room complaints, they manually:
- opened bypass valves
- kept 3-way valves in MAN 100%
- adjusted balancing valves without referencing design flow
- bypassed BMS auto control to “help” the AHU cool faster
4. Impact on Pharma Operations
a. Room Temperature Instability
Excessive flow through the coil → coil gets colder → thermostat overshoots → reheat coil activates → energy waste.
b. High Relative Humidity
Due to unstable coil temperature → dehumidification cycle breaks.
c. Pressure Cascade Failure
Rooms dipped in pressure because:
- AHU supply CFM dropped due to wet coils
- doors could not maintain differential pressure
- impacted Grade D and uncontrolled areas
d. Loss of Chiller Efficiency
Return water temperature dropped due to bypass → chiller ran at low ΔT → higher energy consumption.
e. Near-Deviation Event
One batch drying operation almost failed humidity acceptance criteria.
Deviation was avoided but required documented justification.
5. Diagnostic Findings
- Bypass valves found 50–70% open in 16 AHUs.
- 3-way valves kept in manual mode at 100%.
- DP across coils was fluctuating from 0.6 to 2.2 kPa (0.06–0.22 mbar).
Note: measured differential was very low — consistent with excessive bypass/short-circuiting of flow. Typical chilled-water coil pressure drops are roughly 5–50 kPa in normal designs; high-flow designs may approach 20–100 kPa (AHRI guidance). - Coil ΔT was consistently low (2–3°C).
- Chiller return temperature was 9.5°C instead of 12°C.
6. Root Cause Analysis (Operational)
- Operators believed bypass is required to ‘keep water circulating’.
- Operators manually interfered with BMS valve commands.
- Lack of training on 2-way/3-way valve control logic.
- No SOP for chilled water valve operation.
- No monitoring or alarm for valve manual override in BMS.
7. Corrective Actions Implemented
a. Restore Correct Valve Operation
- Closed all unnecessary bypasses.
- Switched all 3-way valves back to AUTO mode.
- Re-set balancing valves to design flow.
b. Implement BMS Controls
- Enabled alarms for valve manual override.
- Added trend logs for CHW flow, ΔT, valve position.
c. Operator Training
- Trained technicians on:
- valve logic
- effect of bypass on ΔT
- pharma HVAC compliance requirements
d. SOP Implementation
Created an SOP:
- no manual override without Engineering Manager approval
- bypass valves must remain fully closed unless maintenance activity
8. Results (Post-Correction)
Within 1 week:
| Parameter | Before | After |
|---|---|---|
| Coil ΔT | 2–3°C | 6–7°C |
| Room RH variation | ±12% | ±3% |
| Temp fluctuation | ±3°C | ±0.8°C |
| Pressure cascade issues | Frequent | None |
| Chiller power | Increased | 7–9% reduction |
Production rooms passed subsequent validation without deviations.
9. Key Learning for Pharma Facilities
- Bypass ≠ stability.
- Manual override leads to loss of control & GMP non-compliance.
- Operator-created instability is more common than design errors.
- Valve logic must remain under BMS with defined SOPs.

Excellent case study.